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Davis–Besse Nuclear Power Station
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Key Information
Davis–Besse Nuclear Power Station is an 894 megawatt (MW) nuclear power plant, located northeast of Oak Harbor, Ohio, United States. It has a single pressurized water reactor. Davis–Besse is operated by Vistra Corp.
Throughout its operation, Davis–Besse has been the site of several safety incidents that affected the plant's operation. According to the Nuclear Regulatory Commission (NRC), Davis–Besse has been the source of two of the top five most dangerous nuclear incidents in the United States since 1979.[3] The most severe occurring in March 2002, when maintenance workers discovered corrosion had eaten a football-sized hole into the reactor vessel head.[4][5] The NRC kept Davis–Besse shut down until March 2004, so that FirstEnergy was able to perform all the necessary maintenance for safe operations. The NRC imposed an over $5 million fine, its largest fine ever to a nuclear power plant, against FirstEnergy for the actions that led to the corrosion. The company paid an additional $28 million in fines under a settlement with the United States Department of Justice (DOJ).[4]
Davis–Besse was expected to close in 2020 as it is no longer profitable to run when competing against natural gas plants.[6] Plans were updated indicating possible shut down by May 31, 2020.[7] However, Ohio House Bill 6 was signed into law in July 2019 which added a fee to residents' utility bills that funded subsidies of $150 million per year to Davis–Besse and the Perry Nuclear Generating Station to keep both plants operational.[8][9][10] The bill was alleged to be part of the Ohio nuclear bribery scandal revealed by the United States Department of Justice (DOJ) in July 2020.[11][10]
Location and history
[edit]The power station is located on the southwest shore of Lake Erie about 10 miles (16 km) north of Oak Harbor, Ohio and is on the north side of Highway 2 just east of Highway 19 on a 954-acre (386 ha) site in the Carroll Township. The plant only utilizes 221 acres (89 ha), with 733 acres (297 ha) devoted to the Ottawa National Wildlife Refuge. The entrance to the Magee Marsh Wildlife Area[12] is approximately 5 miles east of the power station. The official name according to the U.S. Energy Information Administration is the Davis–Besse Nuclear Generating Station. It is the 57th commercial power reactor to commence building in the United States of America (construction began on September 1, 1970) and the 50th to come on-line July 31, 1978.[13] The plant was originally jointly owned by Cleveland Electric Illuminating (CEI) and Toledo Edison (TE) and was named for former TE Chairman John K. Davis and former CEI Chairman Ralph M. Besse.

Unit One is an 879 MWe pressurized water reactor supplied by Babcock & Wilcox. The reactor was shut down from 2002 until early 2004 for safety repairs and upgrades. In 2012 the reactor supplied 7101.700 GWh of electricity.[14]
In 1973, two more reactors were also ordered from Babcock & Wilcox. However, construction on Units Two and Three never commenced, and these two units were officially canceled in 1981.[15]
Electricity production
[edit]| Year | Jan | Feb | Mar | Apr | May | Jun | Jul | Aug | Sep | Oct | Nov | Dec | Annual (Total) |
|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
| 2001 | 659,778 | 601,935 | 655,630 | 634,920 | 658,726 | 633,332 | 648,532 | 655,159 | 637,346 | 624,363 | 615,007 | 659,590 | 7,684,318 |
| 2002 | 664,299 | 257,171 | -4,123 | -4,136 | -3,264 | -3,616 | -3,665 | -1,052 | -2,868 | -2,879 | -2,910 | -2,865 | 890,092 |
| 2003 | -3,229 | -3,011 | -3,515 | -3,314 | -4,344 | -4,228 | -7,123 | -4,102 | -18,422 | -5,997 | -3,193 | -9,682 | -70,160 |
| 2004 | -22,203 | -24,463 | 48,988 | 616,820 | 654,538 | 635,521 | 656,635 | 550,253 | 636,241 | 662,232 | 644,274 | 663,959 | 5,722,795 |
| 2005 | 333,513 | 395,132 | 669,279 | 640,760 | 661,392 | 635,065 | 647,321 | 651,779 | 633,822 | 591,221 | 632,360 | 664,441 | 7,156,085 |
| 2006 | 663,170 | 593,863 | 95,136 | 20,897 | 641,900 | 625,721 | 662,730 | 662,215 | 574,727 | 672,039 | 489,047 | 670,121 | 6,371,566 |
| 2007 | 668,923 | 601,820 | 639,963 | 643,498 | 630,043 | 640,493 | 661,833 | 658,993 | 629,766 | 663,599 | 646,539 | 620,332 | 7,705,802 |
| 2008 | -6,155 | 297,934 | 662,611 | 637,980 | 668,821 | 631,100 | 667,935 | 674,678 | 654,173 | 682,609 | 662,497 | 589,102 | 6,823,285 |
| 2009 | 684,652 | 617,619 | 680,913 | 264,381 | 679,928 | 652,887 | 675,845 | 674,620 | 654,194 | 681,912 | 659,961 | 682,700 | 7,609,612 |
| 2010 | 681,476 | 561,079 | -952 | -1,365 | -754 | 17,204 | 669,076 | 672,403 | 654,037 | 679,747 | 569,433 | 683,708 | 5,185,092 |
| 2011 | 530,909 | 608,350 | 679,484 | 649,596 | 674,584 | 650,651 | 669,594 | 670,660 | 645,742 | -1,655 | -1,643 | 552,625 | 6,328,897 |
| 2012 | 682,506 | 640,509 | 676,545 | 657,443 | 111,026 | 368,266 | 671,108 | 674,097 | 654,386 | 678,297 | 621,933 | 677,776 | 7,113,892 |
| 2013 | 680,984 | 615,339 | 681,159 | 658,601 | 676,769 | 627,419 | 399,908 | 672,379 | 652,538 | 676,252 | 658,784 | 679,696 | 7,679,828 |
| 2014 | 664,720 | -1,310 | -1,933 | -2,049 | 488,603 | 652,873 | 675,643 | 674,824 | 655,160 | 680,229 | 660,600 | 681,809 | 5,829,169 |
| 2015 | 682,138 | 615,646 | 679,650 | 657,153 | 592,037 | 653,796 | 674,575 | 675,160 | 642,915 | 679,625 | 658,375 | 682,821 | 7,893,891 |
| 2016 | 627,509 | 544,477 | 417,821 | -752 | 457,391 | 646,852 | 667,664 | 666,426 | 370,218 | 659,647 | 658,798 | 678,085 | 6,394,136 |
| 2017 | 678,210 | 587,017 | 675,612 | 654,031 | 672,376 | 609,098 | 669,451 | 670,979 | 650,244 | 674,261 | 656,854 | 677,280 | 7,875,413 |
| 2018 | 677,499 | 587,101 | 110,504 | 658,777 | 677,003 | 652,759 | 672,925 | 671,524 | 651,877 | 678,299 | 660,812 | 681,191 | 7,380,271 |
| 2019 | 618,699 | 615,242 | 680,076 | 657,639 | 677,666 | 653,008 | 671,001 | 673,169 | 572,934 | 677,455 | 659,759 | 680,811 | 7,837,459 |
| 2020 | 662,767 | 497,614 | 80,585 | 644,305 | 677,539 | 650,290 | 669,007 | 671,791 | 653,716 | 679,261 | 660,108 | 681,080 | 7,228,063 |
| 2021 | 682,989 | 617,369 | 679,866 | 655,488 | 672,213 | 650,332 | 585,691 | 650,390 | 651,170 | 665,185 | 658,172 | 610,276 | 7,779,141 |
| 2022 | 680,675 | 505,835 | 64,192 | 237,329 | 659,465 | 651,990 | 671,667 | 670,635 | 652,660 | 678,774 | 659,119 | 359,992 | 6,492,333 |
| 2023 | 681,308 | 616,035 | 682,419 | 658,746 | 678,165 | 652,624 | 672,339 | 672,860 | 653,155 | 678,292 | 659,495 | 680,290 | 7,985,728 |
| 2024 | 680,082 | 636,547 | 73,343 | 651,301 | 674,438 | 649,154 | 669,754 | 670,168 | 650,562 | 675,560 | 657,241 | 679,973 | 7,368,123 |
| 2025 | 679,610 | 613,535 | 676,274 | 654,182 | 675,447 | 648,877 | 667,431 | -- |
Incident history
[edit]1977 first stuck-open pilot-operated relief valve
[edit]On September 24, 1977, the relief valve for the reactor pressurizer failed to close when the reactor, running at only 9% power, shut down because of a disruption in the feedwater system.[17]
This incident later became a precursor to the Three Mile Island accident, in which a pilot-operated relief valve also became stuck open, leaking thousands of gallons of coolant water into the basement of the reactor building.[18]
1985 loss of feedwater event
[edit]On June 9, 1985, the main feedwater pumps, used to supply water to the reactor steam generators, shut down. A control room operator then attempted to start the auxiliary (emergency) feedwater pumps. These pumps both tripped on overspeed conditions because of operator error. This incident was originally classified an "NRC Unusual Event" (the lowest classification the NRC uses) but it was later determined that it should have been classified a "site area emergency".[19]
1998 tornado
[edit]On June 24, 1998, the station was struck by an F2 tornado.[20] The plant's switchyard was damaged and access to external power was disabled. The plant's reactor automatically shut down at 8:42 pm and an alert (the next to lowest of four levels of severity) was declared at 9:18 pm. The plant's emergency diesel generators powered critical facility safety systems until external power could be restored.[21][22]
2002 reactor head hole
[edit]
In March 2002, plant staff discovered that the borated water that serves as the reactor coolant had leaked from cracked control rod drive mechanisms directly above the reactor and eaten through more than six inches[23] (150 mm) of the carbon steel reactor pressure vessel head over an area roughly the size of a football (see photo). This significant reactor head wastage on the exterior of the reactor vessel head left only 3⁄8 inch (9.5 mm) of stainless steel cladding holding back the high-pressure (~2155 psi, 14.6 MPa) reactor coolant. A breach most likely would have resulted in a massive loss-of-coolant accident[citation needed], in which reactor coolant would have jetted into the reactor's containment building and resulted in emergency safety procedures to protect from core damage or meltdown. Because of the location of the reactor head damage, such a jet of reactor coolant might have damaged adjacent control rod drive mechanisms, hampering or preventing reactor shut-down. As part of the system reviews following the accident, significant safety issues were identified with other critical plant components, including the following:
- the containment sump that allows the reactor coolant to be reclaimed and reinjected into the reactor;
- the high pressure injection pumps that would reinject such reclaimed reactor coolant;
- the emergency diesel generator system;
- the containment air coolers that would remove heat from the containment building;
- reactor coolant isolation valves; and
- the plant's electrical distribution system.[24]
The resulting corrective operational and system reviews and engineering changes took two years. Repairs and upgrades cost $600 million, and the Davis–Besse reactor was restarted in March 2004.[25] To replace the reactor vessel head, FirstEnergy purchased one from the mothballed Midland Nuclear Power Plant in Midland, Michigan.[26]
The NRC determined that this incident was the fifth-most dangerous nuclear incident in the United States since 1979,[3] and imposed its largest fine ever—more than $5 million—against FirstEnergy for the actions that led to the corrosion.[4]
Criminal prosecutions
[edit]In January 2006, First Energy, the owner of Davis–Besse, acknowledged a series of safety violations by former workers, and entered into a deferred prosecution agreement with the United States Department of Justice (DOJ). The deferred prosecution agreement related to the March 2002 incident. The deferment granted by the NRC were based on letters from Davis–Besse engineers stating that previous inspections were adequate. However, those inspections were not as thorough as the company suggested, as proved by the material deficiency discovered later. In any case, because FirstEnergy cooperated with investigators on the matter, they were able to avoid more serious penalties. The company paid $28 million under a settlement with the Justice Department.[4] $23.7 million of that were fines, with an additional $4.3 million to be contributed to various groups, including the National Park Service, the U.S. Fish and Wildlife Service, Habitat for Humanity, and the University of Toledo as well as to pay some costs related to the federal investigation.[27]
Two former employees and one former contractor were indicted for statements made in multiple documents and one videotape, over several years, for hiding evidence that the reactor pressure vessel was being corroded by boric acid. The maximum penalty for the three was 25 years in prison. The indictment mentions that other employees also provided false information to inspectors, but does not name them.[27][28] In 2007, one of these men was convicted and another acquitted of hiding information from and lying to the NRC. Another jury trial in 2008 convicted the remaining engineer of similar crimes.[29]
2003 slammer worm computer virus
[edit]In January 2003, the plant's private network became infected with the slammer worm, which resulted in a five-hour loss of safety monitoring at the plant.[30][31]
2008 discovery of tritium leak
[edit]The NRC and Ohio Environmental Protection Agency (Ohio EPA) were notified of a tritium leak accidentally discovered during an unrelated fire inspection on October 22, 2008. Preliminary indications suggest radioactive water did not infiltrate groundwater outside plant boundaries.[32]
2010 replacement reactor head problems
[edit]During a scheduled refueling outage in 2010, ultrasonic examinations performed on the control rod drive mechanism nozzles penetrating the reactor vessel closure head identified that two of the nozzles inspected did not meet acceptance criteria. FirstEnergy investigators subsequently found new cracks in 24 of 69 nozzles, including one serious enough to leak boric acid.[33][34] Crack indications required repair prior to returning the vessel head to service. Control rod drive nozzles were repaired using techniques proven at other nuclear facilities. The plant resumed operation in 2010. The existing reactor vessel head was scheduled for replacement in 2011.[35]
2011 shield building cracks
[edit]An October 2011 shutdown of the plant for maintenance revealed a 30 foot long hairline crack in the concrete shield building around the containment vessel.[36]
2012 reactor coolant pump seal pinhole leak
[edit]On June 6, 2012, an approximately 0.1 gpm pinhole spray leakage was identified from a weld in a seal of the reactor coolant pump during a routine reactor coolant system walkdown inspection. The plant entered limited operations, and root cause analysis was undertaken.[37]
2015 steam leak shutdown
[edit]On May 9, 2015, a steam leak in the turbine building caused FirstEnergy operators to declare an 'Unusual Event' and shut the reactor down until repairs could be made.[38] The plant was brought back online and synchronized with the local power grid 3 days later on May 12 after repairs were completed.[39]
Future
[edit]The facility's original nuclear operating license was set to expire on April 22, 2017. In August 2006, FirstEnergy Nuclear Operating Company (FENOC) submitted a letter of intent to renew.[40] The submission date for the application was August 10, 2010. On December 8, 2015, the NRC granted a 20-year license extension to expire on April 22, 2037.[41] On March 31, 2018, FirstEnergy Nuclear Operating Company filed for Bankruptcy protection.[42] Around that time, the company indicated it would close the nuclear plant.[43] In 2019, Ohio lawmakers debated a $9/MWh subsidy to keep Davis–Besse open.[44] House Bill 6 was signed into law on July 23, 2019, and FirstEnergy announced it would refuel Davis–Besse and rescind its deactivation notice on July 24, 2019.[8] It was later learned that the bill itself was a part of a public corruption scheme revealed by the Justice Department in July 2020.[45]
The scheme involved FirstEnergy paying approximately $61 million to the Speaker of the Ohio House of Representatives, Larry Householder, and Matt Borges, Neil Clark, Juan Cespedes and Jeff Longstreth. For this, they were supposed to help pass the bill subsidizing the nuclear plant and prevent its repeal. Householder was found guilty, removed from the Ohio House and sentenced to 20 years in prison. Clark committed suicide. [46]
Seismic risk
[edit]The Nuclear Regulatory Commission's estimate of the risk each year of an earthquake intense enough to cause core damage to the reactor at Davis–Besse was 1 in 149,254, according to an NRC study published in August 2010.[47][48]
Surrounding population
[edit]The Nuclear Regulatory Commission defines two emergency planning zones around nuclear power plants: a plume exposure pathway zone with a radius of 10 miles (16 km), concerned primarily with exposure to, and inhalation of, airborne radioactive contamination, and an ingestion pathway zone of about 50 miles (80 km), concerned primarily with ingestion of food and liquid contaminated by radioactivity.[49]
The 2010 U.S. population within 10 miles (16 km) of Davis–Besse was 18,635, an increase of 14.2 percent in a decade, according to an analysis of U.S. Census data for msnbc.com. The 2010 U.S. population within 50 miles (80 km) was 1,791,856, an increase of 1.4 percent since 2000. Cities within 50 miles (80 km) include Sandusky, Ohio, 22 miles (35 km); Toledo, Ohio 26 miles (42 km); and Detroit, Michigan, 50 miles (80 km) (distance to the city centers).[50]
See also
[edit]References
[edit]- ^ "EIA - State Nuclear Profiles". www.eia.gov. Retrieved October 3, 2017.
- ^ Johnston, Louis; Williamson, Samuel H. (2023). "What Was the U.S. GDP Then?". MeasuringWorth. Retrieved November 30, 2023. United States Gross Domestic Product deflator figures follow the MeasuringWorth series.
- ^ a b Nuclear Regulatory Commission (September 16, 2004). "Davis–Besse preliminary accident sequence precursor analysis" (PDF). Retrieved June 14, 2006. and Nuclear Regulatory Commission (September 20, 2004). "NRC issues preliminary risk analysis of the combined safety issues at Davis–Besse". Archived from the original on October 3, 2006. Retrieved June 14, 2006.
- ^ a b c d NRC (September 2009). "Fact Sheet on Improvements Resulting From Davis–Besse Incident". NRC Fact Sheet.
- ^ United States Government Accountability Office (2006). "Report to Congress" (PDF). p. 1.
- ^ Funk, John (March 28, 2018). "FirstEnergy Solutions will close its nuclear power plants, but is silent on bankruptcy restructuring". The Plain Dealer. Cleveland, Ohio. Retrieved March 29, 2018.
During months of hearings, the company argued that its uncompetitive old coal and nuclear plants would become competitive once the price of natural gas increased. And at that point, customers would see credits on their monthly bills, they argued. Opponents cited federal predictions that natural gas would stay cheap for decades and customers would just keep on paying higher rates.
- ^ Henry, Tom (January 15, 2019). "Davis-Besse nuclear reactor close to full power". The Blade. Retrieved February 3, 2019.
- ^ a b Carson, Daniel (July 24, 2019). "FirstEnergy Solutions announces it will refuel at Davis-Besse". Fremont News-Messenger. Retrieved July 25, 2019.
- ^ Pelzer, Jeremy (July 23, 2019). "Nuclear bailout bill passes Ohio legislature, signed by Gov. Mike DeWine". The Plain Dealer. Retrieved July 25, 2019.
- ^ a b Wamsley, Laura (July 21, 2020). "Ohio House Speaker Arrested In Connection With $60 Million Bribery Scheme". NPR. Retrieved July 21, 2020.
Last year's nuclear bailout law tacked on a charge to residents' power bills, sending $150 million a year to the nuclear power plants. They are owned by the company Energy Harbor, which was previously known as FirstEnergy Solutions.
- ^ U.S. v. Larry Householder, Jeffery Longstreth, Neil Clark, Matthew Borges, Juan Cespedes, and Generation Now (S.D. Ohio July 16, 2020), Text.
- ^ [1] – Magee Marsh Wildlife Area
- ^ Energy Information Administration (November 2004). "U.S. Nuclear Reactor List – Operational". Archived from the original (XLS) on February 27, 2011. Retrieved June 14, 2006.
- ^ IAEA PRIS database http://www.iaea.org/PRIS/CountryStatistics/ReactorDetails.aspx?current=676
- ^ "Davis-Besse". Archived from the original on April 5, 2018. Retrieved April 5, 2018.
- ^ "Electricity Data Browser". www.eia.gov. Retrieved January 7, 2023.
- ^ Walker, Samuel J. (2004) Three Mile Island: A Nuclear Crisis in Historical Perspective. Berkeley: University of California Press. p 68.
- ^ Behr, Peter; Greenwire. "Three Mile Island still haunts U.S. nuclear industry - NYTimes.com". archive.nytimes.com. Retrieved April 24, 2023.
- ^ Nuclear Regulatory Commission. "Information Notice 85-80". Retrieved June 14, 2006.
- ^ United States Senate. "U.S. Senate Committee on Environment & Public Works Hearing Statements". Archived from the original on June 30, 2006. Retrieved July 7, 2006.
- ^ Nuclear Regulatory Commission. "News Release III-98-040". Retrieved July 7, 2006.
- ^ Nuclear Regulatory Commission. "News Announcement RIII-98-40a". Retrieved June 14, 2006.
- ^ NRC NUREG/BR-0353, Rev 1, pg 4
- ^ Cleveland Plain Dealer, Problems and solutions, July 16, 2003
- ^ NRC. EA-05-071 – Davis–Besse. April 21, 2005.
- ^ "DAVIS-BESSE NUCLEAR POWER STATION, UNIT 1 - MEETING SUMMARYOF JUNE 4, 2002, TO DISCUSS THE REACTOR PRESSURE VESSELCLOSURE HEAD REPLACEMENT" (PDF). Nuclear Regulatory Commission (NRC). July 2, 2002. Retrieved August 6, 2019.
- ^ a b United States Department of Justice (January 20, 2006). "Firstenergy Nuclear Operating Company to Pay $28 Million Relating to Operation of Davis–Besse Nuclear Power Station". Retrieved June 14, 2006. and "Deferred prosecution agreement between the United States of America and FirstEnergy Nuclear Operating Company" (PDF). January 20, 2006. Archived from the original (PDF) on September 27, 2007. Retrieved June 14, 2006.
- ^ Toledo Blade "Ex-engineer found guilty of concealing Davis–Besse dangers"
- ^ "Former FENOC Employee Convicted for Concealing Information from the Nuclear Regulatory Commission". August 26, 2008. Retrieved February 23, 2021.
- ^ The Register [2] August 20, 2003
- ^ Security Focus [3] Archived October 16, 2006, at the Wayback Machine August 19, 2003
- ^ "Davis–Besse radioactive leak is fixed". The Blade. October 25, 2008.
- ^ "8 more nozzles at Davis-Besse found to be flawed". The Blade. Toledo, OH. May 4, 2010. Retrieved July 27, 2015.
- ^ "Meeting set to discuss Besse reactor-head flaws". The Blade. Toledo, OH. May 15, 2010. Retrieved July 27, 2015.
- ^ Funk, John (June 21, 2010). "FirstEnergy to replace lid on Davis-Besse nuclear power plant". The Plain Dealer. Cleveland, OH. Retrieved July 27, 2015.
- ^ "Davis–Besse's restart proper, company, NRC officials say", Toledo Blade, January 6, 2012, retrieved January 14, 2012
- ^ NRC Event Report 48000, retrieved June 8, 2012
- ^ "Davis-Besse still shutdown due to steam issue". Sandusky Register. Retrieved May 12, 2015.
- ^ Henry, Tom (May 14, 2015). "Davis-Besse expected to be at full power today". The Blade. Retrieved May 18, 2015.
- ^ "FENOC letter of intent for license renewal". August 11, 2006. Archived from the original on October 17, 2007.
- ^ "FIRSTENERGY NUCLEAR OPERATING COMPANY AND FIRSTENERGY NUCLEAR GENERATION, LLC DOCKET NO. 50-346 DAVIS-BESSE NUCLEAR POWER STATION, UNIT NO. 1 RENEWED FACILITY OPERATING LICENSE" (PDF). Nuclear Regulatory Commission.
- ^ "FirstEnergy Solutions - Restructuring". FirstEnergy Solutions Corp. Archived from the original on May 10, 2019. Retrieved May 10, 2019.
- ^ "First Energy Files for Bankruptcy; To Close 4 Nuclear Reactors". Neutron Bytes. April 1, 2018. Retrieved May 10, 2019.
- ^ Pelzer, Jeremy (June 24, 2019). "How (un)profitable are Ohio's two nuclear plants? FirstEnergy Solutions says it can't tell the public". cleveland.com.
- ^ U.S. v. Larry Householder, Jeffery Longstreth, Neil Clark, Matthew Borges, Juan Cespedes, and Generation Now (S.D. Ohio July 16, 2020), Text.
- ^ "FirstEnergy agrees to $20 million settlement in Ohio bribery case".
- ^ Bill Dedman, "What are the odds? US nuke plants ranked by quake risk," msnbc.com, March 17, 2011 [4] Accessed April 19, 2011.
- ^ "Archived copy" (PDF). Archived from the original (PDF) on May 25, 2017. Retrieved May 5, 2017.
{{cite web}}: CS1 maint: archived copy as title (link) - ^ "NRC: Backgrounder on Emergency Preparedness for Nuclear Power Plants". Archived from the original on October 2, 2006. Retrieved December 13, 2013.
- ^ Bill Dedman, Nuclear neighbors: Population rises near US reactors, msnbc.com, April 14, 2011 [5] Accessed May 1, 2011.
External links
[edit]Davis–Besse Nuclear Power Station
View on GrokipediaFacility Design and Specifications
Location and Infrastructure
The Davis–Besse Nuclear Power Station occupies a 954-acre site in Carroll Township, Ottawa County, Ohio, along the southwestern shore of Lake Erie, approximately 21 miles east-southeast of Toledo.[4] The facility is positioned adjacent to the mouth of the Toussaint River, facilitating access to lake water for cooling purposes, with geographic coordinates at 41°35′48″N 83°5′11″W.[5] Infrastructure at the site includes a single pressurized water reactor unit within a reinforced concrete containment structure, a turbine building housing the steam turbine and generator, and support facilities such as administrative buildings and wastewater treatment systems.[6] Cooling is achieved through a once-through system drawing from Lake Erie via an offshore intake crib and conduit, designed for a capacity of 42,000 gallons per minute to minimize thermal discharge velocities.[5] A natural draft cooling tower supplements heat dissipation, while on-site dry cask storage manages spent nuclear fuel. Electrical output connects to the regional grid through American Transmission Systems Incorporated lines at 345 kV and 138 kV voltages, enabling distribution to northern Ohio consumers.[7] The layout emphasizes seismic stability and flood protection, given the lakeshore proximity, with the entire site fenced and monitored for security.[6]Reactor Technology and Capacity
The Davis–Besse Nuclear Power Station houses a single pressurized water reactor (PWR) unit, model DB-1, manufactured by Babcock & Wilcox. This design employs a raised loop configuration, where the steam generators are elevated above the reactor coolant pumps to enhance natural circulation capabilities under low-flow conditions.[8] The reactor core consists of uranium dioxide fuel assemblies arranged in a cylindrical lattice, moderated and cooled by pressurized light water.[9] The unit's licensed thermal power output is 2,817 megawatts thermal (MWt), achieved through power uprates approved by the U.S. Nuclear Regulatory Commission (NRC) over its operational history. This thermal capacity corresponds to a gross electrical output of 925 megawatts electric (MWe) and a net electrical output of 894 MWe after accounting for station service loads.[10] The containment structure is a dry, ambient-pressure type, enclosing the reactor vessel, steam generators, and primary coolant systems to mitigate radiological releases in accident scenarios.| Parameter | Value |
|---|---|
| Thermal Power (MWt) | 2,817 |
| Gross Electrical (MWe) | 925 |
| Net Electrical (MWe) | 894 |
| Reactor Type | PWR (Raised Loop) |
Construction and Initial Operations
Planning and Build Phase
The Davis–Besse Nuclear Power Station was conceived in the late 1960s by the Toledo Edison Company, a subsidiary of Ohio Edison, to address projected increases in electricity demand across northern Ohio amid post-World War II industrialization and population growth. Site selection focused on a 1,000-acre parcel in Ottawa County near Oak Harbor, approximately 21 miles east-southeast of Toledo, chosen for its flat terrain, access to Lake Erie for once-through cooling water intake and discharge, and transmission infrastructure proximity to urban load centers.[8][12] The Atomic Energy Commission (AEC), predecessor to the Nuclear Regulatory Commission, reviewed environmental and safety aspects, granting initial authorization for site preparation work.[13] Formal construction permit application for Unit 1, a Babcock & Wilcox-designed pressurized water reactor, was submitted jointly by Toledo Edison and Cleveland Electric Illuminating Company. The full Construction Permit No. CPPR-80 was issued on March 24, 1971, following AEC evaluation of seismic stability, radiological impacts, and emergency planning.[13][14] Groundbreaking and major site activities commenced on September 1, 1970, under limited work authorization, with Bechtel Corporation contracted as architect-engineer responsible for design, procurement, and oversight of civil, mechanical, and electrical systems.[15][8] The build phase involved excavating foundations for the containment structure, erecting the reactor vessel, and installing steam generators and turbines, amid the era's regulatory shifts toward stricter seismic and safety standards post-1960s earthquake reassessments. Initial plans envisioned two units, with orders placed for additional Babcock & Wilcox reactors, but economic pressures including inflation and financing costs led to cancellation of Units 2 and 3 before substantial work began.[15] Total construction duration spanned eight years, with costs escalating to approximately $2.221 billion in 2007-adjusted dollars due to labor, material price hikes, and design modifications for enhanced safety features like improved containment integrity.[8][12]Commissioning and Startup
The Davis–Besse Nuclear Power Station, Unit 1, received its construction permit from the U.S. Atomic Energy Commission on September 1, 1970, initiating the build phase under primary ownership by Toledo Edison Company.[16] Initial fuel loading for the Babcock & Wilcox-designed pressurized water reactor commenced and was completed on April 27, 1977, marking the transition to pre-operational testing phases.[17] The Nuclear Regulatory Commission (NRC) issued the full-power operating license (Docket No. 50-346) in July 1977, enabling progression to criticality and power operations following verification of safety systems and infrastructure readiness.[10] Initial criticality, the point at which a self-sustaining nuclear chain reaction was achieved at low power levels, occurred on August 12, 1977.[18] This milestone followed extensive zero-power physics testing to validate core reactivity parameters and control rod worthiness, as required under NRC oversight to ensure compliance with technical specifications. Synchronization to the electrical grid followed shortly thereafter on August 28, 1977, allowing initial electricity generation at ascending power levels up to approximately 100% of the reactor's thermal capacity of 2,772 MWt.[10] Power ascension testing, including turbine-generator performance trials and balance-of-plant integration, proceeded through late 1977 and into 1978, confirming operational stability without reported significant anomalies during this period.[17] Full commercial operation commenced on July 31, 1978, at a net electrical capacity of 894 MWe, delivering baseload power primarily to the Ohio grid via Toledo Edison's transmission network.[19] The startup sequence adhered to standard NRC protocols for pressurized water reactors of the era, emphasizing sequential validation of reactor protection systems, emergency core cooling capabilities, and containment integrity prior to unrestricted operations. No major delays or safety violations were documented in primary regulatory records for the commissioning phase, though the overall project timeline reflected typical construction-era challenges such as supply chain dependencies for specialized components.[17][18]Ownership and Management History
Early Ownership under Toledo Edison
The Davis–Besse Nuclear Power Station was jointly owned from its inception by the Cleveland Electric Illuminating Company, holding a 51.4% stake, and the Toledo Edison Company, with a 48.6% share, the latter acting as the initial licensee and operator.[8] The facility, a pressurized water reactor, was named in honor of John K. Davis, former chairman of Toledo Edison, and Ralph M. Besse, former chairman of Cleveland Electric Illuminating.[20] This ownership structure facilitated collaborative development amid the expansion of nuclear capacity in the Midwest during the 1970s. Construction began on September 1, 1970, following planning announcements in 1973, with the project aimed at providing baseload power to serve industrial and residential demands in northern Ohio.[8][21] Under Toledo Edison's operational oversight, the station achieved initial criticality and grid connection in 1977, culminating in the issuance of operating license NPF-3 by the U.S. Nuclear Regulatory Commission on April 22, 1977.[6] Commercial operations commenced on July 31, 1978, marking the plant's entry into full revenue-generating service at an initial net capacity of approximately 894 megawatts electrical.[6][18] Toledo Edison managed routine operations, maintenance, and regulatory compliance during the initial decades, benefiting from the plant's high availability in its early cycles, though subject to the era's industry-wide challenges such as regulatory evolution and fuel loading protocols. Ownership interests remained undivided as tenants in common, with Toledo Edison retaining decision-making authority aligned with its lead role until corporate restructurings in the late 1990s.[22] This period established Davis–Besse as a key asset in Toledo Edison's portfolio, contributing to regional energy reliability without major disruptions reported in foundational records.[20]Transitions to FirstEnergy and Beyond
In 1997, the merger of Ohio Edison Company, which owned Toledo Edison, with Centerior Energy Corporation, parent of Cleveland Electric Illuminating Company, formed FirstEnergy Corp. on November 7, consolidating ownership of the Davis–Besse Nuclear Power Station under the new entity.[23] The plant's operations continued under FirstEnergy Nuclear Operating Company (FENOC), a subsidiary responsible for managing FirstEnergy's nuclear fleet, including maintenance, regulatory compliance, and power generation at the 908-megawatt pressurized water reactor.[15] By the mid-2010s, competitive pressures in deregulated energy markets strained FirstEnergy's nuclear assets, leading to the separation of generation operations into FirstEnergy Solutions Corp. (FES), which assumed ownership of Davis–Besse along with other plants like Perry and Beaver Valley.[20] FES filed for Chapter 11 bankruptcy on March 31, 2018, citing unsustainable economics amid low natural gas prices and subsidy failures, though it secured creditor support to maintain operations without immediate shutdowns.[24] Emerging from bankruptcy on February 27, 2020, FES restructured and rebranded as Energy Harbor Corp., retaining ownership of Davis–Besse with a focus on nuclear generation and retail energy services; the transition preserved jobs and plant viability through debt reduction and equity issuance to creditors.[25] Energy Harbor operated the station amid ongoing challenges, including a 2020 license renewal by the Nuclear Regulatory Commission extending operations to 2037.[26] On March 1, 2024, Vistra Corp. completed its $3.43 billion acquisition of Energy Harbor, announced in March 2023, transferring Davis–Besse to Vistra's portfolio and integrating it into the largest U.S. competitive nuclear fleet with over 6,400 megawatts of capacity.[27] This shift positioned the plant under Vistra's management, emphasizing zero-carbon generation amid rising demand for reliable baseload power.[28]Operational Performance and Contributions
Electricity Generation Records
The Davis–Besse Nuclear Power Station, with a net capacity of 894 megawatts, has demonstrated variable electricity generation performance influenced by maintenance outages, regulatory-mandated inspections, and operational uprates. Annual net generation has ranged from lows around 5.185 million megawatt-hours in periods of extended downtime, such as 2009, to highs exceeding 7.7 million megawatt-hours in years of optimal availability.[4] These outputs reflect capacity factors that have occasionally surpassed 100%, achievable through minor power uprates and efficient fuel utilization beyond nominal ratings during low-demand or testing periods. Notable records include a documented capacity factor of 100.0064% in a specific operating cycle, as reported in plant operating data, highlighting periods of near-continuous full-power generation with minimal forced outages. In 2013, the station achieved approximately 98% capacity factor, outperforming the contemporaneous U.S. nuclear industry average and contributing to elevated annual output.[20] More recently, the three-year average capacity factor for 2022–2024 stood at 91.44%, supporting consistent generation amid ongoing safety enhancements.[29] Lifetime performance, spanning commercial operations since July 31, 1978, has been tempered by incidents like the 2002 reactor vessel head degradation, which extended refueling outages and depressed early capacity factors. Historical data from U.S. Nuclear Regulatory Commission sources indicate peak yearly factors reaching 99% in select post-maintenance cycles.[30] Overall, these records underscore the plant's potential for high-reliability baseload power when corrosion and regulatory issues are proactively managed, though average factors remain below top-performing U.S. peers due to site-specific challenges.[31]Reliability Metrics and Efficiency
The capacity factor of the Davis–Besse Nuclear Power Station, calculated as the ratio of actual electrical energy output to the maximum possible output at continuous full-power operation, represents a core metric for assessing operational reliability and efficiency in baseload power generation.[20] High capacity factors indicate minimal unplanned downtime and effective maintenance practices, enabling consistent energy delivery relative to the plant's 894 MW net capacity.[4] In 2013, Davis–Besse attained a capacity factor of approximately 98%, exceeding the contemporaneous U.S. nuclear fleet average and reflecting robust post-maintenance performance.[20] Recent assessments place it at 91.44% as of 2024 data, aligning with top-quartile industry benchmarks amid ongoing uprates and outage optimizations.[29] Historical capacity factors fluctuated due to extended outages, including those stemming from the 2002 reactor vessel head degradation event, which necessitated prolonged shutdowns for inspections and repairs extending into 2004.[32] Pre-2002 averages hovered in the 70-80% range across cycles, influenced by forced outages and regulatory-mandated improvements, but lifetime figures remain moderated by early operational challenges and the two-year post-2002 hiatus.[33] Post-remediation, annual factors improved markedly, with peaks exceeding 95% in multiple years (e.g., 95%, 91%, 99%, and 97% in sequential cycles documented through the 2010s), attributable to enhanced system health programs and reduced forced outage durations.[33][34] Under the U.S. Nuclear Regulatory Commission's Reactor Oversight Process (ROP), Davis–Besse's performance indicators—encompassing metrics such as unplanned scrams per 7,000 critical hours, safety system functional failures, and mitigating systems unavailability—have predominantly registered as green (acceptable) in quarterly evaluations since 2010.[35] In 2023 and 2024 assessments, the plant sustained the highest ROP performance category, with zero white or higher findings, signaling effective probabilistic risk-informed mitigations and low event-initiated core damage frequency.[36][37] Refueling outages exemplify efficiency gains: the 2018 cycle targeted and completed in under 25 days via streamlined planning and human performance enhancements, compared to prior multi-month durations.[38] Forced outage rates, tracked via industry standards like those from the Institute of Nuclear Power Operations, approached 0% in select monthly periods (e.g., December 1994) and remained below fleet medians post-2000s reforms, minimizing capacity losses from equipment failures.[39]| Metric | Recent Value (2023-2024) | Historical Context | Source |
|---|---|---|---|
| Annual Capacity Factor | 91.44% | 98% (2013 peak); 70-95% variable pre/post-2002 | [29] [20] [33] |
| Unplanned Scrams per 7,000 Critical Hours | Green (0 events) | Improved from elevated pre-2002 levels | [35] |
| Refueling Outage Duration | <25 days (2018) | Multi-month historically; reduced via "Drive for 25" initiative | [38] |
| ROP Overall Category | Highest (Green) | Achieved consistently since 2010s reforms | [36] |
